Standby Efficiency

Standby Efficiency - 115VAC

Standby Efficiency - 230VAC

The standby efficiency results are not particularly noteworthy, other than pointing out that power consumption is very low when there is no load placed on the power supply. We measured just 0.6W with 115VAC and 1.07W with 230VAC, which is a pretty good result.

Efficiency


When it comes to efficiency, the Blue Lightning 600W quite frankly blew our socks off. By all appearances, this is your everyday midrange power supply... we simply could not believe getting efficiency results as high as 85%! In fact, the efficiency is above 80% over almost the entire range which can not only save money on electrical costs but is also generally a good indicator of power supply quality. European users (and the other 230VAC countries) will get above 80% efficiency with loads ranging from 60W all the way up to 600W, while 115VAC users will get above 80% up until about 500W.

PFC


The Power Factor Correction was a bit unusual with this power supply. We're used to seeing nice curves at 100VAC and 115VAC, but the 115VAC doesn't rise as quickly as were used to seeing. It's only at 30% and above that the curve begins to rise, but then it stops again at around 60% load and stays at 0.986. 230VAC even starts to drop slightly at maximum load. This isn't an ideal result, but at the same time PFC isn't necessarily one of the most critical factors in determining power supply quality.

Test Setup and DC Outputs Temperatures, Fan Speed, and Acoustics
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  • Per Hansson - Monday, August 27, 2007 - link

    If you take a DMM and measure the power drop on the actual molex connectors, and not take the results directly from the Chroma how does it look then?

    I suspect you have an exponential increase in resistance which causes the Chroma to display incorrect voltage values... (Because of the cable length from the PSU's connectors and up to your load, including interface boards)

    Sincerely - Per Hansson
  • MrOblivious - Monday, August 27, 2007 - link

    Well that and if this really is a Solytech (Deer) it could just be a flaming hunk of crap.
  • Per Hansson - Monday, August 27, 2007 - link

    Yea, but the voltage resistance issue is something that has been the same for all PSU reviews here at Anand

    When you have this problem with all PSU's you need to realize there is something wrong with your testing equipment, sorry for being so blunt... (Especially since none of the other 2 big sites report the same)

    And yes, some scope readings for this DEER PSU sure would have been interesting (just to make sure to beat the dead horse a bit more)
  • Christoph Katzer - Tuesday, August 28, 2007 - link

    Strange though that the Zippy G1 has nearly the whole time close to to 12.0v. I have seen reports from the companies and they look similar (also the high efficiency) and thus I don't think the resistance will be a big issue.
  • MrOblivious - Tuesday, August 28, 2007 - link

    Are they using a Chroma as well for those test reports? Or are they reading directly at the connector without another interface like the spec calls for?

  • Christoph Katzer - Tuesday, August 28, 2007 - link

    "Every" company in Taiwan uses Chroma for their own evaluations.
  • Per Hansson - Tuesday, August 28, 2007 - link

    Christoph Katzer; The issue is of course not that you are using the Croma, it's a great unit; however, the way you use it will most likely result in incorrect voltage readings

    Due to the fact that the resistance in the cables loading the unit will most likely result in a exponential increase in resistance, therefore the results shown by the Chroma will be incorrect, and more incorrect as the load increases and the resistance exponentially increases...

    Just putting a multimeter on an unloaded Molex connector, or, directly on the molex connector you are loading (and not further down where the chroma reads the voltage) would quickly prove or disprove my theory
  • mindless1 - Thursday, August 30, 2007 - link

    You are correct, that a high enough current on too low a wire gauge does cause significant voltage drop, I have observed it many times myself particularly with some of the poorer PSU using 12V connectors with less than 18 ga. wires.

    However, similarly we can't just take the reading from an unused molex connector instead, as a PSU is spec'd to provide it's voltages at the load through the existing wiring harness. It is not necessary to try to evenly distribute that load across all the wire pairs in that harness as that is a practically impossible scenario for implementation running a system, so a bit of a derating factor is needed to appoximate the typical expected loads. IMO, a good start would be loading each supply wire at about 6A (not counting ground returns) up until the rating per rail is met, leaving some supply wires per rail unused when (sum of rail wires * 6A) > rated current per rail. Obviously some connectors and leads are more robust and necessary than others, for example a floppy connector should just be ignored while the 2 x n 12V CPU connector should always be used.
  • mindless1 - Thursday, August 30, 2007 - link

    I meant, high enough current on too high, too small a wire gauge.
  • JarredWalton - Tuesday, August 28, 2007 - link

    But wouldn't regular PC components drawing power from a PSU result in the same sort of increase in resistance? (Note: I'm not at all an electrician, so I could be wrong. Just asking a question.)

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